As kids
most of you glued plastic models together such as jet planes, Old Ironsides,
the Nautilus, and so on. Full size trucks are not much different, at
least some parts of certain models. Major truck body parts like whole
hoods with integral fenders may be molded in two or three section and
adhesively bonded together.
I ran into a problem with the bonds
which held heavy truck hoods together. The right and left halves of
these heavy truck hoods with integral fenders were molded of sheet molding
compound (SMC) which is a thermosetting plastic resin containing about
30 percent by volume of chopped glass fibers randomly oriented for reinforcement.
The raw material comes in soft, pliable sheets that are cut to size,
laid into molds, compressed to shape and thickness, and heated to cure
into rigid complex shapes. These shapes, such as the right and left
halves of a truck from the bumper to the windshield, are then bonded
together with a thermosetting adhesive. The lap joint is typically at
least 25 mm (1 in.) wide. The adhesive is supposed to spread throughout
the joint area when the two parts are brought together and then is supposed
to cure, holding the parts together. The parts in question were made
by a first tier supplier and shipped to a truck assembly plant for final
assembly into vehicles.
The
problem showed itself in the field where fleets of
new trucks were falling apart.
Failures of the adhesive bond can
occur from several causes including unclean surfaces, lack of adhesive,
precure of the adhesive if the parts are not put together soon enough,
and spring back of the parts if they are not clamped into position during
the cure. The problem I ran into was compounded by all of these causes,
not just one. Contamination could never be ruled out because of the
shipping and handling routine. Adhesive was applied by hand with things
like caulking guns so that areas could be missed in a hurry up routine.
Workers could take a cigarette break between the application of the
adhesive and the joining of parts. Because the parts were not clamped
but simply set aside, gravity and mismatch could cause parting of the
adhesive line in the adhesive curing at room temperature. And, compounding
the problem still further, a relatively rapidly polymerizing adhesive
was used so that the parts would not have much time to sag apart before
curing. This attempt to circumvent the spring back problem (without
the use of clamping jigs) exacerbated the precure problem if there were
assemble delays.
The problem showed itself in the
field where fleets of new trucks were falling apart. Failure rates up
to 40 percent were experienced. Since these heavy trucks were supposed
to be durable for industrial jobs, the truck company's reputation was
on the line. To complicate the situation, the first tier supplier was
secretly repairing adhesive bonds in the field without informing the
warranty arm of the truck company. When we found out, we calculated
the actual loss to the truck company at $250 000 a year plus a large
multiple for damage to reputation.
The most obvious solution, namely
to change processes or to change suppliers, was complicated by contractual
obligations and the time to renegotiate and plan, probably two years.
The situation was so bleak that that truck company management had issued
an edict declaring the use of adhesively bonded SMC parts to be infeasible
in manufactured products. The next step would have been an order to
stop production, bringing heavy truck production to a screeching halt.
The threat of this action was real as was its implementation.
At that time, it was obvious that
an NDT method was necessary, there was not one available. The truck
company wanted to be able to test bonded truck bodies as they arrived
at the assembly plant and to retrofit such inspections into the first
tier supplier's plant. The truck company wanted a field portable method
for obvious reasons.
At that point, the only test method
available to the truck company was a gross test for the absence of adhesive.
A feeler gage shim was used as a probe between the two layers of SMC
to detect whether adhesive was missing. The test proved ineffectual
because many truck hoods were observed with the edges of adhesive joints
buttered over with extra adhesive, which prevented the entry of the
shim. Sawing up these hoods revealed that the adhesive was missing from
within the joints. Besides, the shim method did not address the question
of weak bonds containing adhesive.
The plastics design group of the
truck company assembled a task force and looked up as many NDT methods
and instruments as they could find, they but got no definitive off the
shelf answers. They came to me as head of the NDT research, development,
and applications group to evaluate these leads or to invent a new method.
I put Gilbert Chapman, II, on the
job, and he singled out an ultrasonic instrument as having potential.
This was the Sondicator Mk II, which was manufactured at that time by
Automation Industries and has now been redesigned by Zetec. The instrument
used lamb waves at approximately 25 kHz propagating between two closely
spaced probe tips. Actually, the wave motion involved both propagating
waves and evanescent waves analogous to resonance near the tips. The
received signal was compared in both amplitude and phase with the input
signal by means of built-in circuitry, and poor bonds were signaled
by a red light and an audible tone burst. The instrument required calibration
against acceptable reference standards of adhesively bonded material.
The device was immediately found
to be capable of differentiating between well adhered adhesive in the
lap joints and the lack of adhesive over moderate areas, including buttered
over vacant regions. However further work was required to detect the
present but nonadhered adhesive and also adhesive with weak bond(s).
Chapman made a breakthrough on this
challenge by making one important discovery. The instrument would reject
almost all industrially made bonds if it was calibrated against perfectly
made bonds in the laboratory. In reality, many of the industrially made
bonds were strong enough to survive in the field. The test in this stage
of development would have rejected all of production. Chapman's conclusion
was that the perfect laboratory calibration standard was worthless.
It followed that he had to create a calibration standard containing
the requisite degree of imperfection to just barely accept bonds and
reject the bonds that were actually made but unacceptably weak.
Chapman solved the problem of the
creation of sufficiently imperfect reference standards by applying statistics
to a large family of bond samples made in the supplier's factory by
hourly personnel under production conditions. These samples Chapman
tested and rank ordered with the instrument modified to give quantitative
read out, not just the red light and tone burst no go alarm of its regular
operation. Physical tensile pull tests then determined the instrument
level corresponding to the rejectable strength level. The reference
standard was born as the type of sample just good enough to exceed the
minimum specifications of the pull test. With the reference standard,
the no go test could be used.
Chapman then taught the method at
the plant where the trucks were assembled. The truck company also instructed
the first tier supplier on the use of the method and taught its own
quality assurance surveillance agents to use the method so that high
quality could be assured at the supplier and so that the nonconforming
product would not be shipped to the assembly plant.
The quality management office of
the truck manufacturer accepted the method after Chapman wrote it up
in the standard format. The method then served to define a specification
for an adequate adhesive lap join on a per unit length basis. No such
specification had existed in the industry previously. The Chapman specification
is now accepted as an exact parallel to the spot weld specification
for steel.
The edict declaring adhesively bonded
SMC to be infeasible in a manufacturing context was rescinded just weeks
before the order to stop truck production was to have been issued. One
can imagine the magnitude of disruption that would have occurred if
the company had been forced to revert to steel truck bodies. It would
have impacted the plastics industry, the company's stamping plants,
steel sheet orders, fuel economy, corrosion lifetimes of bodies, and
all the future designs for a variety of SMC parts for further trucks
and cars. As feasibility of adhesive bonding of SMC was reestablished,
the use of SMC was extended to other parts and other car lines, thus
improving corporate average fuel economy mileage and durability. The
rescuing of SMC and the elimination of all the above problems is directly
attributable to NDT applied with imagination and the requisite degree
of smarts.
The cost of NDT for keeping the
SMC bonding process under surveillance for a year was about $25 000
including wages and the cost of the instrument. The first tier SMC supplier
reduced its failure rate from 40 percent to five percent simply because
it became cognizant that it could be monitored by the NDT police function.
Other parts went into production in later years because their bonding
quality could be assured. NDT paid for itself many times over.
The references contain articles
by Gilbert Chapman, II, on the method he developed as well as an economic
analysis by Emmanuel Papadakis. For further study of proper management
of NDT in industry and for further study of the cost of quality when
detrimental conditions occur, one would be advised to take short courses
on quality, finances, and NDT.

Figure 1
A Ford LTL-9000 heavy truck with a molded sheet molding compound
(SMC) hood. The adhesive bonding problem occurred in the L-9000
series. The solution to the problem permitted the illustrated truck
and many other models to be built with SMC.
References
Chapman, G.B., II, "Nondestructive Inspection for Quality Assurance
of Fiber Reinforced Plastic Assemblies," Paper No. 820226, SAE Transactions,
Vol. 91, 1982, pp. 887-896.
Chapman, G.B., II, "A Nondestructive
Method of Evaluating Adhesive Bond Strength in Fiberglass Reinforced
Plastic Assemblies," STP 749, Philadelphia, PA, American Society for
Testing and Materials, 1983, pp. 32-60.
Chapman, G.B., II, "Practical NDI
for Fiber-Reinforced Plastics," Materials Engineering, October
1982, pp. 72-73.
Chapman, G.B., II, E.P. Papadakis,
and F.J. Meyer, "A Nondestructive Testing Procedure for Adhesive Bonds
in FRP Assemblies," Body Engineering Journal, Fall 1964, pp.
11-22.
Ford Manufacturing Staff, Ford Laboratory
Test Method FLTM BU 17-1, "Nondestructive Inspection (NDI) of Adhesive
Bonds," Dearborn, MI, Ford Motor Co., July 27, 1980.
Papadakis, E.P., "The Deming Inspection
Criterion for Zero of 100 Percent Inspection," J. Quality Technology,
Vol. 17, No. 3, July 1985, pp. 121-127.